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Case Study

Technologies in Middle East plan for offshore project

Discover how Halliburton's applications configure 179 trajectories targeting reservoir beneath another operator's reservoir in crowded field in Middle East.

Case Study

First application of BaraXtreme fluid in HTHP gas well

Customized drilling fluid system helps successfully deliver well with 7” liner installed to target depth resulting in project cost savings in Malaysia.

Case Study

North Sea operator trial innovative P&A barrier verification

ClearTrac™ Tractor System deploys Shale Barrier Assessment Tools in highly deviated well section proving technique to save around 34 hours of rig time.

Case Study

VersaFlex expandable liner hanger system overcomes challenge

Operator in Brazil saves $200k in rig time with no HSE incidents or NPT, utilizing VersaFlex ELH system to significantly enhance operational efficiency.

Case Study

BaraShale® fluid system reaches wells with incident-free casing

Discover how Halliburton's BaraShale lite fluid system helps save 2 wells both reaching a depth of 9,765 feet deep with the help of 7-5/8" casing incident-free.

Case Study

Operator saves 21 hours on two extended-reach horizontals

Discover how Halliburton's SPECTRUM® Service enables an operator in the Bakken Field to mill and then complete a frac eProfile for completion optimization.

Case Study

Well integrity analysis extends field life in north sea

Discover how Halliburton's expertise in evaluating well integrity proves critical for managing mature field production and extending well life in the North Sea.

Case Study

Slimline ESP system achieves increase in pressure drawdown

Halliburton's slimline ESP system effectively produced fluid from a flowing bottomhole pressure from roughly 1600 psi to 400 psi in Laramie County, Wyoming.

Case Study

Operator achieves 90% intake pressure drawdown of GOR well

Discover how Halliburton's proposed design of ESP system draws fluid levels down from over 5,000 PSIA to under 500 PSIA, a 90% intake pressure drawdown.

Case Study

Twelve rig time hours saved from valve - Case study

Discover how Halliburton's eRED ball valve has been used successfully in previous platform operations taking place in the United Kingdom and other locations.

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